Invoking TIOCVHANGUP on 8250_mid port on Ice Lake-D and then reopening
the port triggers these faults during serial8250_do_startup():
DMAR: DRHD: handling fault status reg 3
DMAR: [DMA Write NO_PASID] Request device [00:1a.0] fault addr 0x0 [fault reason 0x05] PTE Write access is not set
If the IRQ hasn't been set up yet, the UART will have zeroes in its MSI
address/data registers. Disabling the IRQ at the interrupt controller
won't stop the UART from performing a DMA write to the address programmed
in its MSI address register (zero) when it wants to signal an interrupt.
The UARTs (in Ice Lake-D) implement PCI 2.1 style MSI without masking
capability, so there is no way to mask the interrupt at the source PCI
function level, except disabling the MSI capability entirely, but that
would cause it to fall back to INTx# assertion, and the PCI specification
prohibits disabling the MSI capability as a way to mask a function's
interrupt service request.
The MSI address register is zeroed by the hangup as the irq is freed.
The interrupt is signalled during serial8250_do_startup() performing a
THRE test that temporarily toggles THRI in IER. The THRE test currently
occurs before UART's irq (and MSI address) is properly set up.
Refactor serial8250_do_startup() such that irq is set up before the
THRE test. The current irq setup code is intermixed with the timer
setup code. As THRE test must be performed prior to the timer setup,
extract it into own function and call it only after the THRE test.
The ->setup_timer() needs to be part of the struct uart_8250_ops in
order to not create circular dependency between 8250 and 8250_base
modules.
Fixes: 40b36daad0 ("[PATCH] 8250 UART backup timer")
Reported-by: Lennert Buytenhek <buytenh@arista.com>
Tested-by: Lennert Buytenhek <buytenh@arista.com>
Reviewed-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Signed-off-by: Ilpo Järvinen <ilpo.jarvinen@linux.intel.com>
Link: https://lore.kernel.org/r/20220922070005.2965-1-ilpo.jarvinen@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Some platforms can be designed in a way so the UART port reference clock
might be asynchronously changed at some point. In Baikal-T1 SoC this may
happen due to the reference clock being shared between two UART ports, on
the Allwinner SoC the reference clock is derived from the CPU clock, so
any CPU frequency change should get to be known/reflected by/in the UART
controller as well. But it's not enough to just update the
uart_port->uartclk field of the corresponding UART port, the 8250
controller reference clock divisor should be altered so to preserve
current baud rate setting. All of these things is done in a coherent
way by calling the serial8250_update_uartclk() method provided in this
patch. Though note that it isn't supposed to be called from within the
UART port callbacks because the locks using to the protect the UART port
data are already taken in there.
Signed-off-by: Serge Semin <Sergey.Semin@baikalelectronics.ru>
Link: https://lore.kernel.org/r/20200723003357.26897-2-Sergey.Semin@baikalelectronics.ru
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Doing any kind of power management for kernel console is really bad idea.
First of all, it runs in poll and atomic mode. This fact attaches a limitation
on the functions that might be called. For example, pm_runtime_get_sync() might
sleep and thus can't be used. This call needs, for example, to bring the device
to powered on state on the system, where the power on sequence may require
on-atomic operations, such as Intel Cherrytrail with ACPI enumerated UARTs.
That said, on ACPI enabled platforms it might even call firmware for a job.
On the other hand pm_runtime_get() doesn't guarantee that device will become
powered on fast enough.
Besides that, imagine the case when console is about to print a kernel Oops and
it's powered off. In such an emergency case calling the complex functions is
not the best what we can do, taking into consideration that user wants to see
at least something of the last kernel word before it passes away.
Here we modify the 8250 console code to prevent runtime power management.
Note, there is a behaviour change for OMAP boards. It will require to detach
kernel console to become idle.
Link: https://lists.openwall.net/linux-kernel/2018/09/29/65
Suggested-by: Russell King <rmk+kernel@armlinux.org.uk>
Signed-off-by: Andy Shevchenko <andriy.shevchenko@linux.intel.com>
Link: https://lore.kernel.org/r/20200217114016.49856-6-andriy.shevchenko@linux.intel.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit e490c9144c ("tty: Add software emulated RS485 support for 8250")
introduced support to use RTS as an rs485 Transmit Enable signal.
So far the only drivers taking advantage of it are 8250_omap.c and
8250_of.c.
We're about to make use of the feature in 8250_bcm2835aux.c as well.
The bcm2835aux differs from omap chips by inverting the meaning of RTS
in the MCR register. Moreover, omap achieves half-duplex mode by
disabling the RX interrupt and clearing the RX FIFO when TX stops.
The bcm2835aux requires disabling the receiver instead.
Support these behavioral differences by generalizing the rs485 emulation:
Introduce ->rs485_start_tx() and ->rs485_stop_tx() callbacks in struct
uart_8250_port, provide generic implementations containing the existing
code and use them as callbacks in 8250_omap.c and 8250_of.c.
start_tx_rs485() is idempotent in that it recognizes whether RTS is
already asserted. Achieve the same by introducing a tx_stopped flag in
struct uart_8250_em485. This may even perform a little better on arches
where memory access is faster than mmio access.
Signed-off-by: Lukas Wunner <lukas@wunner.de>
Cc: Matwey V. Kornilov <matwey@sai.msu.ru>
Link: https://lore.kernel.org/r/5ac0464ae4414708e723a1e0d52b0c1b2bd41b9b.1582895077.git.lukas@wunner.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The SUPPORT_SYSRQ ifdeffery is not nice as:
- May create misunderstanding about sizeof(struct uart_port) between
different objects
- Prevents moving functions from serial_core.h
- Reduces readability (well, it's ifdeffery - it's hard to follow)
In order to remove SUPPORT_SYSRQ, has_sysrq variable has been added.
Initialise it in driver's probe and remove ifdeffery.
In contrast to 8250/8250_of, legacy_serial on powerpc does fill
(struct plat_serial8250_port). The reason is likely that it's done on
device_initcall(), not on probe. So, 8250_core is not yet probed.
Propagate value from platform_device on 8250 probe - in case powepc
legacy driver it's initialized on initcall, in case 8250_of it will be
initialized later on of_platform_serial_setup().
Cc: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Cc: Paul Mackerras <paulus@samba.org>
Cc: Michael Ellerman <mpe@ellerman.id.au>
Cc: linuxppc-dev@lists.ozlabs.org
Signed-off-by: Dmitry Safonov <dima@arista.com>
Link: https://lore.kernel.org/r/20191213000657.931618-6-dima@arista.com
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Based on 1 normalized pattern(s):
this program is free software you can redistribute it and or modify
it under the terms of the gnu general public license as published by
the free software foundation either version 2 of the license or at
your option any later version
extracted by the scancode license scanner the SPDX license identifier
GPL-2.0-or-later
has been chosen to replace the boilerplate/reference in 3029 file(s).
Signed-off-by: Thomas Gleixner <tglx@linutronix.de>
Reviewed-by: Allison Randal <allison@lohutok.net>
Cc: linux-spdx@vger.kernel.org
Link: https://lkml.kernel.org/r/20190527070032.746973796@linutronix.de
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When a serial port gets faulty or gets flooded with inputs, its interrupt
handler starts to work double time to get the characters to the workqueue
for the tty layer to handle them. When this busy time on the serial/tty
subsystem happens during boot, where it is also busy on the userspace
trying to initialise, some processes can continuously get preempted
and will be on hold until the interrupts subside.
The fix is to backoff on processing received characters for a specified
amount of time when an input overrun is seen (received a new character
before the previous one is processed). This only stops receive and will
continue to transmit characters to serial port. After the backoff period
is done, it receive will be re-enabled. This is optional and will only
be enabled by setting 'overrun-throttle-ms' in the dts.
Signed-off-by: Darwin Dingel <darwin.dingel@alliedtelesis.co.nz>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Currently, we export serial8250_rx_chars, which does a whole bunch of
reads from the 8250 data register, without any form of flow control
between reads.
An upcoming change to the aspeed vuart driver implements more
fine-grained flow control in the interrupt handler, requiring
character-at-a-time control over the rx path.
This change exports serial8250_read_char to allow this.
Signed-off-by: Jeremy Kerr <jk@ozlabs.org>
Tested-by: Eddie James <eajames@linux.vnet.ibm.com>
Tested-by: Joel Stanley <joel@jms.id.au>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Previously the timers where based on the classic timers, giving a too
coarse resolution on systems with configs of less than 1000 HZ.
This patch changes the rs485 timers to hrtimers.
Signed-off-by: Rafael Gago Castano <rgc@hms.se>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Expose set_ldisc() function so that it can be overridden with a
platform specific implementation.
Signed-off-by: Ed Blake <ed.blake@imgtec.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Add an IrDA UART capability flag and change the type of
uart_8250_port.capabilities to be u32 rather than unsigned short to
accommodate the additional flag.
Signed-off-by: Ed Blake <ed.blake@imgtec.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Implementation of software emulation of RS485 direction handling is based
on omap_serial driver.
Before and after transmission RTS is set to the appropriate value.
Note that before calling serial8250_em485_init() the caller has to
ensure that UART will interrupt when shift register empty. Otherwise,
emultaion cannot be used.
Both serial8250_em485_init() and serial8250_em485_destroy() are
idempotent functions.
Signed-off-by: Matwey V. Kornilov <matwey@sai.msu.ru>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Commit ed71871bed ("tty/8250_early: Turn serial_in/serial_out into
weak symbols") made these routines weak to allow platform specific
Big endian override
However recent updates to core, specifically ebc5e20082 ("serial:
of_serial: Support big-endian register accesses") and 6e63be3fee
("serial: earlycon: Add support for big-endian MMIO accesses") means
that round about way to overide the early serial accessors is no longer
needed.
Cc: Jiri Slaby <jslaby@suse.cz>
Cc: Peter Hurley <peter@hurleysoftware.com>
Cc: Rob Herring <robh@kernel.org>
Cc: Kevin Cernekee <cernekee@gmail.com>
Acked-by: Noam Camus <noamc@ezchip.com>
Signed-off-by: Vineet Gupta <vgupta@synopsys.com>
Reviewed-by: Peter Hurley <peter@hurleysoftware.com>
Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>